Well Miller mills FIV and restores access for Aker BP in the North Sea Challenge

1712 X 963- JNO202598 2

Well type

Producer

Max. depth:

85˚5,775 meters (operation)

Max. pressure:

1,624 psi.

Max. temp.

101°C / 214°F

Background

Milling interventions can resolve downhole problems for a variety of restrictions, not just scale buildup. One such issue is downhole hardware becoming stuck or no longer functioning properly.

In early 2020, Aker BP experienced a significant increase in water cut from a horizontal producer.

Production logging tools found no scale problem, but the run did reveal a half-open formation isolation valve (FIV). An additional caliper log showed the FIV had a clean shifting profile, but, after a failed open-close operation, Aker BP decided to mill the valve to make further logging and water shut off possible.

Welltec® previously collaborated with Aker BP to perform systems testing for just such a scenario in 2018, so the client knew there would be no need for further testing. Aker BP contacted Welltec for help with the operation.

well are reduced, this can be connected to the performance of GLVs, and so a replacement may be required.

In this case, a client in Malaysia needed to carry out several valve replacements, with the added challenge of highly deviated intervals in three wells. Use of standard slickline would not be enough to overcome the deviations of 84° – 85°.

As the client had previous experience with Welltec®, they were extremely confident in the capabilities of the personnel and equipment to perform each operation. With other intervention providers unable to reach the target depth (TD), the Well Tractor® would be needed to deliver the Intervention.

Operation

Welltec deployed a 318 Well Miller® conveyed by a 318 Well Tractor®. A 414 Well Cleaner® Power Suction Tool was also mobilized as a contingency for potentially fishing half-moon pieces. The Well Tractor would also facilitate plug setting.

During the milling run, after tagging the FIV, Welltec milled the valve in two three-hour stages, pumping 50L of fluid every 30 minutes. Welltec milled the FIV and collected two half-moons in a single run.

Achievements

Welltec overcame this challenging operation and delivered access below the FIV for Aker BP.

Welltec completed the milling operation in just 8.5 hours, representing cost and time savings for the operator.

Welltec Tractor hero

Well Tractor®

The original tractor with 30 years of experience

- Well Miller for Hardware Milling Hero

Well Miller®

for Hardware Milling

Well Cleaner Power Suction Tool Hero

Well Cleaner®

Power Suction Tool

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