Pulling of stuck monolock plug on e-line

1920X1080 Pulling Of Stuck Monolock Plug On E Line

Total depth

11,165 ft

Max. temperature

284°F (140°C)

Max. pressure

393 bar

Deviation

Vertical

Background

An operator in Nigeria had attempted to pull a monolock plug on slickline in a vertical oil well, but during the operation the plug became stuck at 11,165 ft (3,403m). Despite jarring 66 times with up to 1,800 lbs of force, it wasn’t possible to retrieve the monolock plug.

Based on Welltec’s successful milling of a stuck safety valve 10 days earlier on a neighboring well, the operator asked Welltec® to come up with a solution to retrieve the monolock plug.

Operation

Using standard, readily available equipment Welltec mobilized to the well site with the Well Stroker®. Unfortunately the first run encountered problems resulting in a fish on top of the plug. After an unsuccessful slickline fishing attempt, Welltec was able to retrieve the fish using a JD fishing tool on e-line. Once this hindrance was removed, the way was clear to retrieve the stuck plug.

The Well Stroker in combination with the Welltec Release Device® and a GS pulling tool successfully pulled the monolock plug free on the next run. The plug continued to be troublesome on its way to surface, as it became partially stuck twice taking, a series of up-strokes to retrieve it.

Achievements

The operation took a total of two days.

Operator very pleased with how Welltec embraced their safety culture. Operator now considers Welltec as preferred choice in well intervention. The pulling force of the Well Stroker is superior to slickline:

It can anchor and apply up to 33,000 lbs of force directly to the problem.
Eliminates risk of parting and LIH slickline cable.

Products applied

Well Stroker

Well Stroker®

For actuation

Welltec Release Device (WRD) Hero

WRD®

Welltec® Release Device

Well Key GS Pulling Tool - 1920X1080

Well Key® GS Pulling Tool

For fishing operations

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